PERILAKU LENTUR SAMBUNGAN MODEL TAKIK PADA BALOK APLIKASI UNTUK BETON PRACETAK

ABSTRACT: Precast  concrete  was  better  than  cast  in  situ  reinforced  concrete  in  particular  fast  and  mass  work.    Precast concrete was already used but the system has connection problem.  The research objective was know bending behavior of  notch  system  connection.    The  research  use  full  scale  simple  beam  with13  representativestrain  gauge  and  11 dial gauge (tranducer). The beam was loaded vertical  reversal loading with implemented increase gradually untill maximum load and than continous monotonic loading until the beam failure.  After that the beam was break open to watch bar and concrete  condition after  loading  examination.  Research  product  shown  that.  most  strictly  SNI(Indonesion  National Standart) condition can reached with 4,66 mm displacement and 17,326 tf loading at elastic beam condition.  First crack become  at  6,64  tf  loading  that  is  equal  with 86,8%  static  loading  calculation.    Maximum  loading  was  23,99  tf  or  62% static  loading  calculation,  it  was appropriate  with  fatigue    theory  that  reversal  loading  decrease  40-55  %  from  static loading.  First crack was bending crack and than the crack was develop diagonal type.  Type of crack was appropriate with cast in situ reinforced concrete.
Keywords: precast concrete, bending, notch, reversal
Penulis: Chatarina Niken
Kode Jurnal: jptsipildd080009

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